Date: | Thursday 26 July 1984 |
Time: | 16:58 LT |
Type: | Boeing 727-232 |
Owner/operator: | People Express Airlines |
Registration: | N518PE |
MSN: | 20641/936 |
Year of manufacture: | 1973 |
Total airframe hrs: | 30025 hours |
Engine model: | P&W JT8D-15 |
Fatalities: | Fatalities: 0 / Occupants: 105 |
Other fatalities: | 0 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Buffalo, NY -
United States of America
|
Phase: | Approach |
Nature: | Passenger - Scheduled |
Departure airport: | Newark, NJ (KEWR) |
Destination airport: | Buffalo, NY (KBUF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING THE DEPARTURE FROM NEWARK, NJ, THE AIRCREW NOTED A VIBRATION WHICH CEASED AFTER THE GEAR WAS RETRACTED. THE CREW SUSPECTED THAT A TIRE WAS OUT-OF-ROUND OR A GEAR DOOR WAS VIBRATING & CONTINUED THE FLT. DURING THE APCH TO BUFFALO, NY, THE VIBRATION OCCURRED AGAIN WHEN THE LANDING GEAR WAS EXTENDED, BUT CEASED ON FINAL APCH. THE APCH & LANDING WERE CONTINUED WITHOUT FURTHER INCIDENT. AFTER LANDING, AN EXAM OF THE ACFT, GEAR & GEAR DOORS REVEALED NO REASON FOR THE VIBRATION. HOWEVER, DURING THE FLT, A PIECE OF THE LEFT TRAILING EDGE FLAP HAD SEPARATED. IT HAD SEPARATED ON FINAL APCH & HAD HIT A PARKED CAR CAUSING MINOR DAMAGE. THERE WAS EVIDENCE OF IMPROPER SURFACE PREPARATION & BONDING DURING A PREVIOUS REPAIR OF THE FLAP.
Probable Cause:
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC84IA271 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report
|
|
Sources:
NTSB NYC84IA271
Location
Revision history:
Date/time | Contributor | Updates |
31-Mar-2024 13:14 |
ASN Update Bot |
Added |
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